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Doug Gordon (M) from
Pontiac, Michigan
USA
(Comp Nr/Finish:
349 ) |
1975 - Category: AFUELDRAG, Type: XN, Class: A/FD, Div: 3 |
"Purple Haze II" Owned by Doug Gordon
from
Pontiac, Michigan
USA
| Crew Chief: Steve Best |
'72 Dragster by
Wayne Farr |
Powered by Injected Nitro 433 Chevrolet with
direct drive |
1/4 Mile ET: |
7.061 at NHRA Indianapolis IN 9/01/75 |
1/4 Mile MPH: |
193.54 at NHRA Indianapolis IN 9/01/75 |
1000 FT ET: |
Unknown at Unknown |
1000 FT MPH: |
Unknown at Unknown |
1/8 Mile ET: |
Unknown at Unknown |
1/8 Mile MPH: |
Unknown at Unknown |
|
Entry's 1975 Performance Ratings (0 to 100) based on comparison to average ET/MPH:
|
1/4 Mile Rating: ET 73.01,
MPH 52.25 |
Entry is 0.96594 times average ET and 1.00280 times average MPH |
1000 FT Rating: ET 00.00,
MPH 00.00 |
Entry is 0.00000 times average ET and 0.00000 times average MPH |
1/8 Mile Rating:
ET 00.00,
MPH 00.00 |
Entry is 0.00000 times average ET and 0.00000 times average MPH |
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1975 Records: |
1/4 Mile: 6.769 ET, 205.02 MPH |
1000 Ft. 0.000 ET, 0.00 MPH |
1/8 Mile: 4.790 ET, 0.00 MPH |
1975 Average: |
1/4 Mile: 7.310 ET, 193.00 MPH |
1000 Ft. 0.000 ET, 0.00 MPH |
1/8 Mile: 4.940 ET, 0.00 MPH |
1975 Minimum: |
1/4 Mile: 7.851 ET, 180.72 MPH |
1000 Ft. 0.000 ET, 0.00 MPH |
1/8 Mile: 5.270 ET, 0.00 MPH |
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Racer's Web Site |
No video link |
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Notes: Ran 7.21 at Sanair Drag Strip 8/75. Ran 7.061 to qualify 25th at 75 US Nats. Car was former "Bob's Drag Chutes" top fueler.rnThe team's finest hour with the Purple Haze II was the WCS meet at Cayuga Dragway in Cayuga, Ontario. They had low qualifier, winner of Pro Comp, and recipient of the "Best Appearing Car" award! The team was riding high for a long time after that.rnBack at the Grandnationals in Montreal, the team again made a good run to qualify for the field. Unfortunately, a piece of the mallory metal that was used to balance the crank broke loose and exited through the oil pan, also dinging up the engine's bottom end. This is as close as the team ever came to actually "blowing an engine." They were able to fix the pan and clean out the other shrapnel, but decided against trying to make a hard run with an unbalanced crankshaft, so withdrew on Sunday morning.rnShortly after this, the reality hit that we simply could not afford the price of being truly competitive on a national NHRA level. - Doug Gordon webpage |
Submitted by Draglist Archives, Last updated on Wednesday, August 6, 2025, 05:31:39 PM by
John Murnan II.
Approved by Super Crew. |